[1]滕學清,楊向同,朱金智,等.YK3井套管斷裂原因分析[J].石油管材與儀器,2019,5(05):77-82.[doi:10.19459/j.cnki.61-1500/te.2019.05.017]
 TENG Xueqing,YANG Xiangtong,ZHU Jinzhi,et al.Analysis of Casing Fracture Cause in YK3 Well[J].Petroleum Tubular Goods & Instruments,2019,5(05):77-82.[doi:10.19459/j.cnki.61-1500/te.2019.05.017]
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YK3井套管斷裂原因分析
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《石油管材與儀器》[ISSN:2096-0077/CN:61-1500/TE]

卷:
5
期數:
2019年05期
頁碼:
77-82
欄目:
失效分析與預防
出版日期:
2019-10-20

文章信息/Info

Title:
Analysis of Casing Fracture Cause in YK3 Well
文章編號:
2096-0077(2019)05--0077-06
作者:
滕學清1楊向同1朱金智1呂拴錄12楊成新1
1.中國石油塔里木油田公司 新疆 庫爾勒 841000;2.中國石油大學材料科學與工程系 北京 100249
Author(s):
TENG Xueqing1 YANG Xiangtong1 ZHU Jinzhi1 LYU Shuanlu12 YANG Chengxin1
1.PetroChina Tarim Oil Field Company, Korla, Xinjiang 841000, China; 2.Material Science and Engineering Department of China University of Petroleum, Beijing 102249, China
關鍵詞:
套管鉆頭鉆塞遇阻鐵屑斷裂
Keywords:
casing bit drilling cement plug resistance iron remains fracture
分類號:
TE925.2
DOI:
10.19459/j.cnki.61-1500/te.2019.05.017
文獻標志碼:
A
摘要:
對YK3井套管鉆塞遇阻事故進行了調查研究,對鉆水泥塞過程中返出的鐵屑和鉆頭損壞形貌進行了分析,依據鉆頭和鐵屑形貌確定套管失效形式為斷裂。對影響鉆塞遇阻的各種因素進行了分析,結果表明:套管斷裂導致鉆塞遇阻。對套管失效時間分析結果表明,在正注水泥碰壓之后、鉆塞之前,套管已經斷裂。對固井工藝進行了分析,找到了固井施工存在的問題。通過分析計算套管在固井過程中的受力狀態,確定固井過程中套管沒有過載,套管斷裂與其材料本身存在的原始缺陷和交變載荷有關。建議進一步研究固井過程中套管受力狀態,并對該批剩余套管進行檢驗。
Abstract:
This paper gives an investigation on accident of drilling hard trip in Well YK3. The casing fracture failure form was found per analyzing on morphology of iron remains from well bottom and failure bit morphology. It was shown that the casing fracture resulted in the drilling cement plug resistance pass through analysis on accident cause. It was concluded that the casing broke before drilling cement plug and behind bump plug during injection cement. Some problems in well cementing process were found per analyzing well cementing technology. It was confirmed that casing was not overloaded, and casing fracture may be caused due to itself material original defect and alterantingload by calculating load born on the casing in cementing process. It was suggested that load born on casing in well cementing should be studied, and the casing left should be inspected.

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備注/Memo

備注/Memo:
第一作者簡介:滕學清,男,1965年生,高級工程師,1989年畢業于中國石油大學(華東)鉆井專業,主要從事石油鉆井和完井工程技術工作。E-mail: [email protected]
更新日期/Last Update: 2019-10-25
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